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THE USE OF CHLORINATED SOLVENTS AS WASHING AGENTS IN THE METAL AND STEEL INDUSTRIES, AND PARTICULARLY IN THE PRODUCTION OF BRASS POINTS FOR WRITING INSTRUMENTS, WITH ASSOCIATED PROBLEMS
Second Section
Problems related to the use of chlorinated solvents in the production and utilisation of tips for ball-point pens.
The first part of this document has provided a broad illustration of metal degreasing methodologies and of the problems that might arise in the utilisation of chlorinated solvents.

This second part will analyse the practical implications of a number of problems recently emerged in the production of refills.

At the beginning of 1993, talking to a solvent technician working for a multinational company in the sector of chlorinated solvent production, we learnt that two years ago approximately all chlorinated solvent manufacturers had to give up the use of stabilisers like 1,4-dioxan because of toxicological problems. Such stabilisers were deemed highly toxic because of their very dangerous vapours.

Moreover, dioxan is considered noxious to the mucous (eyes and lungs) and is absorbed by the skin.

All the problems occurred in the production of refills all over the world which caused a lot of troubles to both users and manufacturers date back to that period, but only very recently an explanation could be found.

All industrial sector using chlorinated solvents to degrease metals ran into the same problems.

The identification of their cause was neither simple nor immediate; solvent manufacturers did not have sufficient information at their disposal and the problem was totally unprecedented. Up to that moment REINOL had never encountered problems in the use of inks for ball pens.

Several tests were carried out both internally and by external laboratories to come to a correct data interpretation. They were made necessary by the far-reaching implications of the issue and by the difficulty in finding a solution.
Analysis of the first anomalies occurred and search for the cause of writing blocking.
The first complaints arrived in July 1991; a Korean customer complained for the presence of defective refills: they usually started to write, but after a while, the writing specimen became irregular until it totally stops.

By insisting on moving them some refills started to write and became gradually normal again.

The stop of writing into the refills is normally due to the following reasons:

1) The ink thickens and increases viscosity.

To check this instance, our laboratory measured viscosity with a computerised viscometer Haake Rotovisco Rv-20 equipped with a PK5-1.0 probe.

Thanks to this equipment our laboratory is able to carry out the analysis of ink viscosity even with a limited number of refills.

The ink of these defective refills revealed value in compliance with the warranted characteristics.

2) Ink crystallisation.

We analysed at the microscope a counter sample of ink sent back by the customer, but no crystallisation was observed; the ink on the slide was limpid and pure with no alteration.

3) Formation of a plug at the bottom of the tube due to a wrong ink formulation or to an early ageing on ink itself.

All tests carried out excluded the possibility that ink might have formed a dry plug at the bottom of the tube (in this case the consistency of ink was always normal) and also excluded the formation of corrosion in the tip shoulder area.

The latter observed at the microscope always appeared perfectly clean and free from any oxidation (see
picture n. 1).

In this respect it is worth remembering that raw materials used in the production of inks are made of chemically pure compounds and their formulas are by their very nature constant and invariable; in the opposite case, their specific features would be totally upset.

In the case of dyes, for instance, the substance colour depends on the specific arrangement of atoms in the molecule.

All coloured organic substances are unsaturated compounds, that reduced with hydrogen loose their colour.

A few cases will now be illustrated to better explain the above-mentioned concepts:


Phtalic Imide Isatin


In this case it was enough to change the arrangement of the -NH group and the carbonyl group (>C=O) to completely modify the characteristics of the product obtained (phtalic imide is colourless whilst isatin is orange).


Yellow Colourless Colourless


 

 To check the quality of the ink we replaced a number of tip with new ones and then proceeded to the various ageing tests.

All refills treated this way could write normally.

The only unexplored instance left was ink flowing in the tip internal duct and more specifically the ink close to the ball.

We carried out a new test in our laboratory, we removed the ball and collected the ink on a slide for subsequent observation at the microscope.

The ink turned out to be turbid, with unknown clotted particles.

Our customer carried out a well-structured laboratory test with the following results:

1) The ink analysed at the microscope was limpid.

2) The ink contained in refill tips had white insoluble spots(see Annex A: Customer's "TEST REPORT").

Moreover, tips showed a corroded area on their outer wall as it can easily be observed in
pictures n. 2 and 3.

At the same time, when the first problems arose, our laboratory sent some refills to SGS Laboratories Ecology Department for a more accurate examination.
SGS Ecology
Technical evaluation of possible metal enrichment of ink in contact with brass parts.
Since the defect (writing blocking) was believed to be due to the presence of brass powder not totally extracted during washing, zinc, copper and lead samples were taken from three different areas in the refill.

Three samples were obtained:
  1. in direct contact with the ball
  2. in the bottom part of the tip
  3. in the polypropylene tube at 5-6 cm. from the tip.
The latter was considered the reference sample since it does not come into contact with the metal parts of the refill itself.

The different samples obtained were mineralised with an acid mixture (HCl -HNO3) and a hot process so as to destroy the organic matrix and produce a solution.

To check the presence of metals a plasma spectrophotometer with sequential reading was used.

Results showed (see Table n. 5 and Annex B) a greater concentration of the three metals in the bottom part of the tip which according to the SGS laboratory is due to the presence of brass powder caused by a "non perfect cleaning of the tip after the lathe operations". This powder creates a wider contact surface and increases the likelihood of brass mineralisation. To confirm or reject the assumption put forward by the SGS Laboratory we had to experimentally reproduce the defect in our laboratory.
Table 5
 Parameters C (mg/kg) B (mg/kg) A (mg/kg)
Lead < 0,5 40,9 < 0,5
Copper < 0,5 46,1 < 0,5
Zinc 6,6 67,1 < 0,5


To this aim, we formulated a number of different inks mixing with them some brass powder resulting from the tip lathe operations.

Refills assembled with these mixtures wrote with no defect at all, neither immediately nor after the ageing test.

Given the tiny amount of defective product, the analysis of A samples did not produce reliable results.

At this point, we had to go into greater details using an electronic microscope to find out the nature and origin of the clot inside the tip.
We entrusted the Chemical Laboratory of the Chamber of Commerce in Turin with this task.
With the aim of identifying the nature of the clots which are probably the root cause of the hole obstruction in our brass ball point refills, a scanning electron microscope (JEOL 6400) equipped with an EDS probe was used (X-ray energy dispersion spectrometer TRACOR Z-MAX 30). See Annex C.

The EDS analysis, as it can be easily observed (Chart n. 2 and
Picture n. 18), highlighted as basic elements agglomerates of copper with zinc and chlorine. Their arrangement perfectly overlaps with that of the clot removed from the tip (see Picture n. 4).

In some cases the procedure highlighted only the presence of copper particles and this puzzled operators.

The same instrument was used to measure the various elements present in a brass tip free from corrosion (see Chart n. 1). In this case no particle of chlorine was observed.

After a first microscopic observation with a magnification power of x100, the magnification was increased to 1.500 to assess the crystalline structure of the elements making up the unknown agglomerate (see
Picture n. 5).

Then we started looking for the element with the same crystalline structure observed at the microscope. After the analysis of several pure particles and artificially created products, the optimal result was obtained using some brass powder (see
Picture n. 6).

The size of particles forming the agglomerates is about three micrometers and their crystalline structure matches that of pure electrolytic copper powder.

One of the doubts expressed by our experts referred to a possible contamination of ink at its finale stage, caused by an imperfect purification during the final stages of the production process. This could have led to an accumulation of insoluble particles inside the ball feeding duct during refill centrifugation.

To side-step this problem, one of the first checks carried out at the end of the production process is the centrifugation of some refills assembled with the ink under study. This operation which takes a long time (30 minutes approximately) is followed by a microscope analysis of the ink located behind the ball to verify the actual absence of insoluble parts.

To this purpose our experts prepared an X-ray 120 magnification map of insoluble residues obtained during ink purification at the centrifugation and filtration stage scattered in an area of 0,85 square centimetres (it should be pointed out that REINOL utilises a single process, with two filtrations and one centrifugation stage).

The map (see Annex C) highlights the presence of particles containing iron, silicon, calcium, sulphur and aluminium in a smaller percentage, and just one single copper particle.

If we compare the results of this map with the previous one, we can notice the actual efficacy of the purification process: indeed none of the particles present in residues is found in ink at its final stage.

Based on these results one could think that refills stopped writing because of an excess of brass powder or chips due to an insufficient cleaning and washing; however, the fineness of particles (3 micrometers) and the unusually high quantity could have been traced back to a bad washing of tips, but also to a cause which remained unknown for the moment.

The chlorine found during the EDS analysis (see Chart n. 2) was not taken into account at that stage simply because the hypothesis of corrosion had not been considered yet.
Verification of results and conclusions
Experimental test were needed to reproduce the same circumstances in the laboratory and to check whether the root cause of the writing defect was in brass contamination or in other substances normally used in the ball tip production process and in the subsequent refill assembly.

Inks were therefore contaminated with different percentages of the following products:

- very fine powder obtained from the machining of tips. Due to the greater surface in contact with ink, it is much more reactive than the tip brass;

- new blending oil used for the machining of tips;

- used blending oil with brass chips.

These mixtures were then used in the assembly of some control refills that were subsequently subjected to a number of tests, ageing tests included.

All refills thus obtained and assembled were operating perfectly. This meant that the writing blocking in defective refills was not due to the presence of brass (powder or chips) caused by a bad washing of the tip itself.

Some observations had already led us to think that the final explanation was to be found in a different direction, namely:

- The defect occurred both in tips supplied by experienced and excellent manufacturers and in products supplied by minor manufacturers with little experience in the field.

- The same defects recurred using ink supplied by different manufacturers.

During our study, we received refills from all over the world. They were filled with both our products and with inks supplied by competitors - they all had the same defect.

The time frame could be easily identified and it was the same for all manufacturers.

The EDS analysis clearly highlighted the presence of chlorine particles that do not belong to the composition of brass, nor to the formulation of inks.

The use of unwashed tips, dirty with oil, did not produce any defect, even after one year and a half of tests. Tips remain shiny and clean.

At page 49
Picture n. 7 shows a tip as it usually appears.

Our laboratory was developing a project for a very important customer. For the project it used ink formulated in the laboratory and tips of a very high quality. But there again, after about six months, all assembled refills stopped writing. This was the clue to look for different causes. The defect could no longer be ascribed to a bad ink formulation, that in this case had been produced in the laboratory with the help of precision micro-balances and therefore with an error rate of 0,001 grams for 100 g. of finished products!

The clue to the solution was provided by the observation of a number of tips with clear signs of acid corrosion on the inner duct of new tips coming from different manufacturers as it can be noticed in the following pictures:

- Pictures
n. 8, n. 9, n. 10, n. 11, n. 12, n. 13, n. 14, n. 15

-
Picture n. 24

In this case corrosion is caused by the etching of hydrochloric acid formed through hydrolysis of the chlorinated solvent and is due to phenomena explained in the previous section.

It should be noted that hydrochloric acid is by far the most aggressive in etching brass followed by nitric acid, whilst sulphuric acid produces a weaker effect.

The term brass encompasses a wide range of Copper and Zinc alloys, where the latter is in a percentage not exceeding 50% (usually this percentage varies from 11% to 50%).

Zinc reacts easily to acid and develops hydrogen:

Zn + 2H+ < = > Zn++ + H2

and

Zn + 2HCl < = > ZnCl2 + H2

The greater the amount of impurities in Zinc, the easier the above-mentioned reaction.

Zinc chloride is deliquescent substance, that is a highly hygroscopic salt with the property of turning into a solution by absorbing water from the surrounding atmosphere. This situation highly increases the reactivity of chloride itself.

Even copper melts in any acid if exposed to air.

With hydrogen halide acids, like for instance hydrochloric acid, copper oxide forms insoluble copper salts which precipitate:

2Cu + HCl < = > 2CuCl + H2

This acid etching is followed by the formation of zinc, lead and copper salts.

Brass oxidation and the consequent formation of the so-called "saline efflorescence" leads to the formation of insoluble particles mixed with ink in the duct behind the ball. An example of this acid etching on brass, with the consequent formation of saline crystals, was already registered in nickel-plated tips at the end of the machining process in 1984 (see
Picture n.17).

To avoid this problem, manufacturers started to machine tips only after the nickel-plating process.

In other cases acid etching may be caused by factors not linked to washing products but to the raw materials used during the forming process (
Picture n. 17).

The ensuing copper and zinc oxides are highly reactive to certain ink ingredients and produce insoluble substances, usually copper and/or zinc carboxilates. These compounds alter the normal rheology of the ink, decreasing its ability to flow into the capillary duct.

The degeneration process occurs in three distinct stages:

Stage 1: At this stage a weakening of the writing specimen occurs; it is due to a narrowing of the tip inner duct and therefore to a smaller amount of ink flowing through.

Stage 2: Salts continue to increase with consequent writing "gaps".

Stage 3: It is the final stage of the degeneration process when tips just cease to write altogether.

Some refills however, if subjected to centrifugation, start to write again reasonably well, gradually improving until the ink flowing out has not brought out with it all saline particles.

The salt content of these refills is smaller and has not caused a total duct occlusion yet.

In refills which do not start writing again the salt content has totally blocked the capillary duct.

If we slightly blow the refills, writing starts and gradually becomes normal again. Even after ageing test, the performance of refills processed this way remains normal.

This is in line with the results of some tests carried out by our competitors. They demonstrated that by replacing or washing the tips of defective refills, but using the same ink, the problem did not crop up again.

Furthermore, there is the possibility that in some tip lots, the capillary duct might have already been totally obstructed.

In the light of these data, the results of all the tests carried out by external laboratories fine an easier explanation:

- The high copper and zinc percentage in the tip ink stressed by the SGS analysis confirms the high content of the two metals in ionic form, which therefore passes into ink.

- Copper and zinc particles found in all tests carried out by the Chemical Laboratory of the Chamber of Commerce are in fact Zinc and Copper salts, as it can be easily observed from Charts n. 1 (EDS analysis carried out on a brass tip with no writing defect: no chlorine, copper or zinc particle is found to be part of the brass alloy) and n. 2 (EDS analysis of the waxy clot behind the ball of a tip belonging to a defective refill: the two above-mentioned salts are not only made of copper and zinc, but also of a certain amount of chlorine.

- This explains why replacing the tips of defective refills with new tips all anomalies are avoided.

Corroded tips probably account for a negligible and sporadic part of production.

To check the accuracy of our conclusions, we experimentally reproduced the defect in our laboratory. We dipped for few minutes some etch-free tips in a 0,1 normal solution of hydrochloric acid (which amounts to 3,5 g. of HCl dissolved in a litre of water). After a few days the tips had the same problems of those contained in defective refills; this is clearly shown in
Picture n. 19 and 20.

Over a subsequent set of tests carried out at the Chemical Laboratory of the Chamber of Commerce, we tried to ascertain the origin of saline efflorescence using manifestly defective refills and tips coming from Korea.

Here are the findings of the analysis of saline formations:

1) Brass undergoes a selective oxidation of its components;

2) Displayed saline efflorescence is primarily made of Zinc and Lead salts.

Picture n. 21 and 22 are very helpful in explaining these findings.

At the same time a scanning electron microscope was used to observe a saline formation found in a recently produced tip (see
Picture n. 23).

The EDS analysis clearly shows that this crystal is made of Zinc salts.

Result of the EDS analysis carried out on a new and corrosion-free brass tip.

Result of the EDS analysis carried out on the clot behind the ball of the tip of a defective refill.
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